My 1986 7B I bought from SVOBud is under way. I have been posting pictures in my Albums Section. So far so good. I have removed all the interior pieces and placed them in storage. After spending a day assessing where to start I have focused with great success on the engine. The odd oil pressure Bud had mentioned was due to an ancient oil filter that was solidified choking the engine. Fresh oil and filter and everything went normal. I was also suprised to find the fuel filter was the original. I could tell by the fact the dealer coated it with rust and sound deadener. This was also changed. I ran a computer scan and found the MAF and EGR have failed. The new ones will arrive Friday. I still took it for a drive and the 7B is a rocket. Can't wait till I get the final parts. Stay tuned
There now NGK Iridium. I've had very good results with these in past turbos I have worked on. If they get weird I'll switch to Autolite. I did a compression test today. The results were 159 across all four cylinders exactly. The ford manual I have read online shows that reading to be good. I ordered the new stem seals also. I'm also just about done replacing all the hoses with proper formed ones. The guys at the parts store here are really into this project. We plowed catalogs and measured for 2hours to replace every one. I also have a new waterpump and thermostat. I'm going to finish the head work and timing belt, housing etc and install them last . Should be done next week. The more I work and test this engine the better I feel it will not need a full overhaul in the near future.
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